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Old 05-24-2007, 03:00 AM   #1
Lurch
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Default Really Blown Motor

Removed Bill's Engine Tonight and (Quote All 8 Rod's are broken and Wrist pin and pistons are in the pan ) Note motor still turns over will try and post pitcure's All the Rods broke at the bottom right at the crank.
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Old 05-24-2007, 09:35 AM   #2
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to the motor gods.
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Old 05-24-2007, 01:41 PM   #3
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Here are some pictures of the damage.


Click on the pictures for more detail




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Old 05-24-2007, 01:52 PM   #4
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Here is mine with only 2 broke rods, compared to Bill's with 8 broken.



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Old 05-24-2007, 02:53 PM   #5
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wow!!!!!!!!!
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Old 05-24-2007, 04:35 PM   #6
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those rods got pwnt...and I thought my breaking of 1 rod and piston looked like carnage lol
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Old 05-24-2007, 05:09 PM   #7
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How much boost were your running??? Nasty!!!
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Old 05-24-2007, 08:34 PM   #8
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14 psi.
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Old 05-25-2007, 03:48 AM   #9
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Default Engine

Hello Please read below Post Tks
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Old 05-26-2007, 10:40 AM   #10
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Default Now in English

Hello,
I have the motor completely apart and I have a lot of Questions. I'm going to see if Mike will take me some more pictures with everything apart and post it on nloc. Any possible theoryÔÇÖs besides I blew it up, (HA! HA!) are welcome. Anyone can call me and are welcome to look it over. Once the pictures are posted you will see the rods are still all hooked to the crank and they look like they came loose about a 1/2 inch of each other. Also when I removed the Timing cover there was a freeze plug lying in a little space inside the cover, no dents or scratches. One other strange item the motor is missing a follower or rocker off the intake side.
It showed no code's until we would crack the throttle at idle then it would show a rich mixture on the side missing the rocker which would make since because the exhaust valve would still open and let the fuel go into the exhaust, I know a o2 reads air. Thanks in advance for the help. Sorry I missed the meeting I was motoring. Mory Congratulations on the Lightning can't wait till see it. Mike I will lay all of this stuff out in nice order and get with you I want to post this on nloc and start reading some responses. Thanks to all have a great day and Good night.
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Old 05-26-2007, 11:07 AM   #11
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Default Re: Now in English

Quote:
Originally Posted by Richard H.
Hello,
I have the motor completely apart and I have a lot of Questions. I'm going to see if Mike will take me some more pictures with everything apart and post it on nloc. Any possible theoryÔÇÖs besides I blew it up, (HA! HA!) are welcome. Anyone can call me and are welcome to look it over. Once the pictures are posted you will see the rods are still all hooked to the crank and they look like they came loose about a 1/2 inch of each other. Also when I removed the Timing cover there was a freeze plug lying in a little space inside the cover, no dents or scratches. One other strange item the motor is missing a follower or rocker off the intake side.
It showed no code's until we would crack the throttle at idle then it would show a rich mixture on the side missing the rocker which would make since because the exhaust valve would still open and let the fuel go into the exhaust, I know a o2 reads air. Thanks in advance for the help. Sorry I missed the meeting I was motoring. Mory Congratulations on the Lightning can't wait till see it. Mike I will lay all of this stuff out in nice order and get with you I want to post this on nloc and start reading some responses. Thanks to all have a great day and Good night.
you must be a goose creek Grad
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Old 05-26-2007, 12:00 PM   #12
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Bill,
Thanks for clarifying that. I understood the original post, it just took a couple of reads.
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Old 05-26-2007, 04:01 PM   #13
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Mitch

Give me a call . I'll swing by and take some pictures.

Mike
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Old 05-26-2007, 07:22 PM   #14
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So Richard H. It looks like you are no longer the Lighting Killer than tital now belonges to someone eles!!
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Old 05-26-2007, 11:59 PM   #15
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Default Killer is me

I lurch take full and 99.6% killer, Also the Mechanic though!!
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Old 05-27-2007, 01:45 AM   #16
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I've actually heard of the rockers falling off on the 03-04 Cobra's . It wasn't a common problem but several people had it happen to them and never knew it until the valve cover was pulled . It seems some were just not right from the factory and some were . I honestly wouldn't worry about it .

And looks to me like a a little rod stretch action .
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Old 05-28-2007, 05:52 PM   #17
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Here are some more pictures of the motor apart.

Click on the pictures for more detail








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Old 05-28-2007, 06:03 PM   #18
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That must be one hell of a blender they used
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Old 05-28-2007, 07:21 PM   #19
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Damn! What's the going rate for scrap metal right now?
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Old 05-29-2007, 07:37 AM   #20
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I am just curious as to what made that happen.
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